Szczegóły publikacji

Opis bibliograficzny

Pilot plant results for advanced $CO_2$ capture process using amine scrubbing at the Jaworzno II Power Plant in Poland / Marcin Stec, Adam Tatarczuk, Lucyna Więcław-Solny, Aleksander Krótki, Marek Ściążko, Stanisław Tokarski // Fuel : the science and technology of fuel and energy ; ISSN 0016-2361. — 2015 — vol. 151, s. 50–56. — Bibliogr. s. 55–56, Abstr. — Publikacja dostępna online od: 2015-01-20. — S. Tokarski - afiliacja: TAURON Polska Energia S. A. — 10th ECCRIA : the 10th European Conference on Coal Research and its Applications : 15th–17th September, 2014, [Kingston upon Hull, United Kingdom]

Autorzy (6)

  • Stec Marcin
  • Tatarczuk Adam
  • Więcław-Solny Lucyna
  • Krótki Aleksander
  • Ściążko Marek
  • Tokarski Stanisław

Słowa kluczowe

pilot plantpost combustion CO2 capturecoal fired power plant

Dane bibliometryczne

ID BaDAP118851
Data dodania do BaDAP2019-01-07
Tekst źródłowyURL
DOI10.1016/j.fuel.2015.01.014
Rok publikacji2015
Typ publikacjireferat w czasopiśmie
Otwarty dostęptak
Czasopismo/seriaFuel

Abstract

The purpose of this study is to present the testing of a 30 wt% solution of ethanolamine (MEA) in an advanced CO2 capture pilot plant. The mobile pilot plant, designed, constructed and operated by the Institute for Chemical Processing of Coal (IChPW) in cooperation with industrial partners: TAURON Polska Energia and TAURON Wytwarzanie, was used to carry out trials at the Jaworzno II Power Plant in Poland. Thanks to flexible technological design, numerous process flows sheet modifications were tested. The use of split flow or inter-stage absorber cooling is demonstrated and compared to the standard amine process. Presented modifications resulted in an increase of CO2 recovery ranging from 3% to 8%, whilst reducing the reboiler heat duty by about 5%. The correlation of CO2 recovery, reboiler heat duty and process parameters (solvent loading, L/G ratio) has been established for numerous process flow sheet modifications. The tests provide valuable experimental evidence for modifications described in the literature, mainly through modelling and demonstrate that flow sheet modifications, despite the increase in plant complexity, are worth considering. (C) 2015 Elsevier Ltd. All rights reserved.

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